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Non-manufacturing Applications: Development

8. Case Studies of Six Sigma Improvement Projects

8.2 Non-manufacturing Applications: Development

Korea Heavy Industries & Construction Company (which changed its name to Doosan Heavy Industries Company in 2001) learned Six Sigma management skills from General Electric in 1997, and started Six Sigma to achieve manage- ment innovation. In early 2000, the company published a book called “Six Sigma Best Practices” in which 15 Six Sigma project activities are contained. The long-term vision of the company is to become a “Competitive world-class company of 21st century with the best quality and technology.” To achieve this vision, the company made its own MAP (man- agement action plans), with which CST (critical success themes) were selected for quality and productivity innovation.

This case study presented here is one of the CSTs which is contained in the Six Sigma Best Practices. The Engineering &

Technology Division of this company desired to solve one CST, namely “Reduction of Short Shelf-Life Material (SSLM).” Management formed a project team with a full-time BB and five part-time GBs to tackle this project.

17.00 16.80 16.60 16.40 16.20 16.00 15.80 15.60

0.60[mm]

[mm]

AverageRange

16.54 16.30 16.06

0.44 0.20 0.50

0.40 0.30 0.20 0.10 0.00

(1) Define

There were many materials necessitating storage on a shelf for some period of time to be subsequently used to create var- ious products. Each material had its own specified shelf life- time depending upon whether it was stored in a refrigerator or not. Some frequently used materials and their specifications are listed in Table 8.5. The shelf life-time was counted from the manufactured date.

Table 8.5. Stored materials and their specified shelf

However, due to poor storage conditions and other rea- sons, the shelf life-times became short, and they could not be used in good condition. Such SSLM resulted in some COPQ, environmental pollution and additional testing expenses.

(2) Measure

During the period of July – December, 1999, scrap materi- als were found during the process of manufacturing many products. Table 8.5 shows the scrap materials for the product, stator bar and connecting ring.

Storage in refrigerator Storage in storeroom Material

Shelf life-time Storage

condition Shelf life-time Storage condition Mica paper tape (#77865)

Mica paper tape (#77906) Gl yarn flat tape prepreg Mica M tape (#77921) Modified epoxy varnish Polyester resin–35%

Epoxy impreg fiber cloth (#76579) Pa–polyster sesin

Pb–catalyster Polyester comp

6 months 6 months 1 year 6 months 6 months 1 year 6 months 10 months 10 months

1 year

below 7°C 2–10°C below 5°C

2–10°C below 10°C

2–10°C 2–10°C 2–10°C 2–10°C 2–10°C

3 months 3 months 3 months 2 months 2 months 6 months 1 month 3 months 3 months 3 months

below 23°C 18–32°C 18–32°C 18–32°C 18–32°C 18–32°C 18–32°C 18–32°C 18–32°C 18–32°C

Glass cloth & tape 1 year 2–10°C 3 months below 25°C

Polyester comp

1 year 2–10°C 3 months 18–32°C

Table 8.6. Scrap materials in the stator bar & connecting ring

The products/processes that were of particular concern are listed in Table 8.6 along with their current process capabilities.

Table 8.7. Current process capabilities

(3) Analyze

In order to discover the sources of defects and variation, a cause-and-effect diagram was sketched by the team as shown in Figure 8.9.

Product/process Defect Unit Opportunity Total

Opportunity DPU DPO DPMO

Process capability (sigma level) Stator bar &

connecting ring 61 12 50 600 5.083 0.101 101,667 2.77

Stator W’g ass’y 148 13 71 923 11.385 0.160 160,347 2.49

Lower frame A. 31 14 8 112 2.214 0.277 276,786 2.09

Rotor coil A. 4 17 5 85 0.235 0.047 47,059 3.17

Total 244 1,720 0.142 141,860 2.57

Defect: Over shelf life-time of SSLM

Unit: 4 items categorized in the processing using SSLM Opportunity: Quantities of SSLM used in unit Total opportunity = Unit × Opportunity DPU = Defects/Unit

DPO = Defects/Total opportunity DPMO = DPO/1,000,000

Short-term capability = Long-term capability + 1.5

Scrap Cause of scrap

Material Purchase

quantity Quantity Unit Number of times

Change in manufacturing

schedule

Earlier purchase

No control of storage Etc.

Modified epoxy varnish Epoxy impeg fiber cloth Glass cloth & tape Transposition filler

……

92 7,890 958 4,118

31 120 84 55

GL SH RL LB

2 2 5 1

1 2

1 1

2 1 1

1

Figure 8.9. Cause-and-effect diagram for SSLM

In the past six-month period, the total defect count on the materials was 244, and the Pareto diagram for the types of defects is shown in Figure 8.10.

Figure 8.10. Pattern of defects

Defect Pattern

Lack of control of stock materials

Change in manufacturing

schedule

Strict storage condition

Too many/

small storage materials

Others

Count 103 97 15 14 15

Percent 42.2 39.8 6.1 5.7 6.2

Cum. % 42.2 82.0 88.1 93.8 100.0

Count 250 200 150 100 50 0

Percent 100 80 60 40 20 0

Material Men

Defects

Control Purchase

Too many/small materials (3)

Strict storage condition (3)

Short shelf life time-limit (2)

Lack of information (1)

Lack of concern with SSLM (1)

Not accessible electrically (4) Change in manu.

schedule (3) No observation of

first-in, first-out (1) Lack of control of stock materials (1)

No confirmation of Stock material (1)

Early purchase (1)

Inaccuracy of required data (1)

Figure 8.10 shows that insufficient control of SSLM in the storehouse accounted for 42.2% of the total and the unex- pected changes in the manufacturing schedule were responsi- ble for 39.8% of the total defects.

(4) Redesign

In order to reduce the defects of SSLM, the computerized inventory control system was redesigned to increase the con- trol efficiency of SSLM. The current process after the redesign looks as follows.

In this current process, there is no tool for checking and monitoring SSLM, and no one is assigned for checking the defects. The redesigned and improved process (Figure 8.11) makes cross-checking of the manufacturing schedule in advance possible. Also, the related departments can monitor and control SSLMs through an on-line system.

Figure 8.11. Redesigned process for SSLMs

Reconfirm shop load

Manufacturing

process schedule Concurrently related departments exchange information on

manufacturing schedule BOM

MRP

P/O

Store SSLM in refrigerator

Cross checking of actual manufacturing schedule

Control of SSLMs through data warehouse Manufacturing

process schedule BOM MRP P/O Store SSLM

in refrigerator

Inventory control by documentation

(5) Improve

By practicing the improved process, they could obtain the following data for the first three months after the start of its use for SSLMs.

We can compare the quality performances of the old and newly improved processes as follows, clearly showing the impact of the Six Sigma team activities:

(6) Control

In order to maintain the benefits, the team decided to fol- low the following control procedures:

• Update the SSLM instruction manual, and check the manual every six months.

• Educate the workers on SSLM information every month.

• Monitor related data through the on-line computer sys- tem every other month.

Before improvement After improvement DPMO

Sigma level COPQ

141,860 2.57

$190,000/year

11,510 3.77

$15,400/year (estimated) Product/

process Stator bar &

connecting ring Stator wiring assembly Lower frame A.

Rotor coil A.

Unit

13 7 6 10

Opportunity

24 45 3 5

DPU

0.308 0.429 0.167 0 Total

Defect

4 3 1 0 8

Total opportunity

312 315 18 50 695

DPO

0.01282 0.06667 0.05556

0 0.01151

DPMO

12,820 66,670 55,560 0 11,510

Process capability (sigma level)

3.73 3.00 3.09 6.00 (estimated)

3.77

8.3 R&D Applications: Design Optimization of Inner Shield